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I Forge Iron

Irondragon Forge ClayWorks

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Posts posted by Irondragon Forge ClayWorks

  1. Will do, she was upset because our fur kid Daisy dog got bit by a copperhead and her foot (the dogs) swelled up to twice it's size. A quick trip to the vet was in order. The dog is going to be fine and on a 7 day course of antibiotics to prevent any secondary infection.

    I finished the metal work on the forge. Welded together angle iron channels and welded them to the forge for the fire brick doors. We decided on soft firebrick because we have a lot of it from the kiln's. Also cut some kiln shelf for the floor. I will get some pictures of it running when the sun goes down. Probably will paint it black with 2000 degree high heat paint.

    Front view would anyone believe me if I say I planned the channels to be on an angle?:D

    nxt2rk.jpg

    rear view

    35cr9ea.jpg

     

  2. 1 hour ago, (M) said:

    For this burner or one like it could I get away with a 1-20 or even 1-10 psi propane regulator?

    I doubt that it will be your last burner so go with the 0-30 psi regulator.

  3. 1 hour ago, Frosty said:

    Good grief, I take a day for a club meeting and I miss a pun thread. DRATS! Oh well, complaining is fu tile.

    Your forge is coming along really well What can your better half tell us about using Veegum? What does she think about what we're wanting to try using it for?

    Frosty The Lucky.

    She has only used it in certain pottery glazes and has no idea how it would work when mixed in a castable refractory or IR reflecting wash.

  4. Did you oil it like instructed back in January? Looks to me like the grease may have picked up pieces of bad bearings or gear chips and jammed in the bottom of the teeth. Use a solvent like kerosene and wash out all of the grease with a brush, while working the gears back & forth to see how badly they are worn.

  5. Fired it up a while ago and ran it at 3 psi for a few min. then gradually increased the psi and opened the air choke until it was running at 15 psi. The bubble alunima cured without any problems and it came up to yellow heat pretty quick.

    I took another kiln shelf to block the rear port and found out we will not use kiln shelves for the doors. When the forge was shut off and cooling down we heard a ting and found the shelf to be cracked (sounded just like a blade ting when quenching wrong). So Debi wants to use soft fire bricks in a channel for the doors, that way we wont have to worry about transporting fragile kiln shelves.

  6. May have been good the air bags failed to deploy with all the recalls of Takata air bags that the dealers can't do because of the unavailability of new air bags from the manufacture. Glad everyone is on the mend and "someone" was looking out for them.

  7. Good information to have. I picked up over 400 pounds of cut up sucker rod and have made many anvil hardy's from them. They were cut to about four foot lengths and many of the ends were cut off which I have. Some one put them in the city metal dumpster where I worked and the mayor and shop foreman gave me permission to take anything I wanted. Too bad the city did away with the metal dumpster years ago.

  8. Thanks Mike, the beauty of the cart is it cost 0$, made from all reclaimed materials (cannibalized BBQ grill and some heavy gauge sheet metal from a metal building).

    Today we finished the bubble alunima coating. Had to put a layer about a third of the way up and let it set up then roll the forge and put the top layer in. I found an old pool noodle that fit the burner port so used some as a form to keep the port open. Also solved the secondary air problem a while back. Just had to insert the burner about a quarter inch deeper so now the choke works as it should.

    Will let it cure overnight then fire it up tomorrow to slowly cure it.

    2a8m7vk.jpg

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